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Grumpy ![]() ![]() ![]() ![]() ![]() Group: Advanced Members Posts: 2,722 Joined: 1-January 04 From: Bakersfield CA Member No.: 81 ![]() |
Yep you read it right, one more down (IMG:http://www.frrax.com/rrforum/style_emoticons/default/banghead.gif) The motor didn't lay down on me, but it wasn't right either! I kept getting metal(bronze) out of the breather tank oil on Sat so that told me to cut the first filter open after changing oil at the track. It didn't look bad at all, so I asked around some and everybody said thats normal. So I ran the car on Sun in the second session after adjusting the lifters in the mourning, and it ran fine but seemed down on power like all weekend. Well I did run the car in the 3rd session in 105deg heat with the water at 210 and oil at 280 at 70psi. I drained the oil breather again and it looked bad again, so I put the car on the trailer after just 5(out of 10) sessions on the weekend.
I'm off to talk to the engine shop now........ OH for those that want the BEST brake setup ever, call Steve over at ProStop Performance and get you a 996 setup! I could lockup(ABS) my 315 V710's on any lap any time that I wanted(over braked (IMG:http://www.frrax.com/rrforum/style_emoticons/default/tongue.gif) ) I'm pretty sure the Carbotech XP12's pad's are to much (IMG:http://www.frrax.com/rrforum/style_emoticons/default/rotf.gif) on this setup! The only good thing this weekend...... I picked up 4 used Hoosier(5 sessions) for $12.50 a tire! (IMG:http://www.frrax.com/rrforum/style_emoticons/default/blink.gif) (IMG:http://www.frrax.com/rrforum/style_emoticons/default/2thumbs.gif) |
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Experienced Member ![]() ![]() ![]() Group: Advanced Members Posts: 1,086 Joined: 16-January 04 From: Chandler AZ Member No.: 130 ![]() |
QUOTE WELL I found out what is wrong, THE PISTON SKIRT'S BROKE OFF the bottom of a few pistons! How would this happan? Piston rocking in the bore? Or getting on the throttle too soon before the engine is properly warmed up? That happened to me once. My #6 piston (TRW forged flattop) came out of the bore in two pieces, all while the car ran 13.50s (Gen I SBC 355). |
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Lo-Fi Version | Time is now: 16th June 2025 - 10:46 PM |