The Teal Terror is finally hitting the track again this weekend. 9 cars showing up for CMC at Autobahn County Club.
Bone stock LM4 with F-body pan, intake, manifolds made 263whp on the dyno. New nickname might be "Pig" with the 3340lb minimum weight.
Looks like we can't embed images, so here's a link: https://ibb.co/PtzdDZC
Awesome!
I like this post very much. (I've been saying I should have kept that car and skipped the Corvette and just bought the current convertible and been done with it while owning both).
The car looks great!
Has it been 9 years????
More pics please?
I think I bought the ground control set off that car. They're still treating me well!
Chris, you do have the GC parts from that car. Lol.
3118? We put a shitload of cage in that thing. 🤣🤣🤣
That was a downer weekend. Went out for practice, got one lap and the car shut off into T3, coasted to the back side exit.. Towed it back and found the fuel pump plug fell off the bulkhead connector. Easy fix, plug it back in and the car fired right up.
Went out for qual and got 4 laps in when I felt the engine lay down coming off T2. Looked at the temp gauge and saw 235*, not the end of the world. Looked at the oil pressure and saw 0 psi, hit the ignition switch and coasted to the back side exit.
Towed the car back and the engine is locked up tight. Probably shut it off right before it scattered. It was a junkyard LM4 with 40psi cold idle, IR baffle, 20w50, and 1 quart overfilled. Sucks but that's racing.
https://ibb.co/NNyS25v
Well shit. That really sucks. I was hoping to hear that it made the podium on the first weekend. Sorry to hear that it went sideways....
That car looks nice with the Vette wheels on it! Might have tried those on our B4C, but going with a more stock look, so will use the GTA wheels it came with.
Sorry to hear about the lockup. That sux!
What/Where is the waiver from? Is that from Nasa Tech or CMC?
Congrats getting back out in CMC and sorry for the motor trouble.
It's like being on double secret probation, doesn't exist. Basically, don't crucify the new guy before he gets the go-fast crack pipe firmly in his mouth. Haha
Bob Denton has been trying to get me to race CMC for over a decade. He did most of the drivetrain/plumbing/wiring on the car since I can't find time lately. The Great Lakes gang is a great group of people and gets that the car would be 100% if I could. It weighed/dyno'd right so that's the most important thing.
Everyone is driving the snot out of the cars and it'll probably be a season before I can make the podium anyway. SEAT TIME!
Nobody cares about "cheating" if you're on the tail. That's why you can't even protest someone that's below a certain position in a lot of series.
Update: The saga continues.
Went and got another LM4 from the cheapest junkyard with the plan of Bob doing rings/bearings on it. The first one the yard pulled out wouldn't even turn over. Dad ended up driving to their other yard down the road for one that would turn over. He ran it the two hours to Bob's and they tore it down and immediately noticed it had dropped a valve seat in each head but in a way it was probably "running" but on 6 cylinders. The short block was good but now we needed useable heads.
The junkyard said bring it back and we'll give you a refund or take the locked up one for the heads and bring back two cores to get the $200 core charge. Well, the locked up engine had water in it at some point and the bores were rusty and so were some valves. We were able to get it to move after 2 days of cleaning soaking bores in Deep Creep.
In the mean time, we yanked the locked up engine out of the CMC car and tore it down. Heads were good but it took some work to get the rotating assembly apart. It spun the 3 and 4 rod bearings and spit them out the sides. That's what had it locked up. Crank and two rods are junk. Between all the crap, I should have another good block, crank, set of rods/pistons. Junkyard is getting zero shit back, keep the $200, dickheads.
Bob had the "reman" done a few days later, Dad picked it up and I bolted on the FW/clutch/PP/bellhousing, almost forgot the pilot bearing, knock sensors, last weekend. Dad dropped it in the car with some buddies during the week and hooked up everything top side. I showed up Saturday, stabbed the trans, bolted up DS, exhaust, torque arm. We primed the engine, bolted on accessories, tried to fire and nothing but cranking. Didn't even try to fire. No RPM on scan tool, changed CKP sensor, no change. Checked spark, nada. Checked 12v at coil, yep. Checked power/needed wires at computer, yep 12v. WTF, drop the starter again, check light green on CKP connector, nope, 0V. WTF? Bad computer? Found random internet post on guy saying he jumped 12v to CKP sensor and it fired up. Fuck it, out of ideas, let's get dangerous. Jumped 12V, hit starter button, VROOOOM. Sat there and idled great for 30 minutes. Crossed fingers, shut it off, fired right back up.
No fuckin' clue, but it sounds great, 45lbs hot oil pressure with cheap 10w30 @ 800rpm, no bad noises. Need to button up a few things we ran out of time for but it's looking good for Autobahn in early October.
Huge thanks to Bob for getting this done even with the Championships coming up. And to my Dad for getting all this done so I could try to get my house re-model done before it has a 3rd birthday. LOL.
To be continued...
That's crazy. But progress is good!
I still can't wait to see it on the podium.
I'm thinking maybe you should do something more about oil control. The IR baffle may have helped but not enough. If trackbird can get his stock LS truck to oil starve pulling into the parts store you may have found the culprit on your first engine. Ideally you'd go dry sump.
I have a 3qt Accusump on the shelf. I just haven't had enough spare time for plumbing/mounting.
That reminds me, I ordered a bunch of stuff from Improved Racing and haven't seen it yet. Time to look into that.
It's only been 10 months, I guess I better get around to writing an update...
I got the car back out in October. Huge thanks to my Dad and Bob Denton for junkyard running and freshening an engine in time. We ran the Friday test day and worked out some new cars bugs. There was literally something we had to fix every session. So, it was money/time well spent.
The results for the weekend were GREAT! We took a brand new car that I hadn't ever driven more than a few laps and ran P4, P3, and P2 in 3 races against veteran competitors.
Here's the video of R3: https://youtu.be/vntTYiKNAGI
When I burned out on my World's Longest Home Re-model last winter, I spent some time in the garage fixing a few issues, built a new cooling system with an eBay AL radiator, and had to add 70lbs of "not ballast" to the car.
Dad and I brought the car to Mid-Ohio in May and things were looking pretty promising but we battled issues all weekend before finally getting it right with the last race
R1, I spun in my own water 3 times when the radiator would boil over. I was angry when the checkered flew but happy that I hadn't torn up the car. Remember kids, stock radiator caps belong in the trash.
R2, Car started sputtering in corners and I eventually pulled off. P10. Dropped the tank after the race and found the 1/8" line had come off the Racetronix pump. A little safety wire and hopefully it's a permanent fix.
R3, worked my way to P1 through the race and was barely able to hold on. The tires were used up and Derek Wright was coming hard. Super happy to see the Checkered, the first WIN in this car.
I never got around to editing videos, but hopefully soon.
More to write about Gingerman in June but out of time.
Here's a teaser pic from Gingerman: https://ibb.co/cbwv2M0
Gingerman R3 video, Win #2!: https://youtu.be/55eHjMrCKMc
Damn that looks like fun!
You and No. 30 make good dance partners!
Oh and I think Double Secret Probation would have been over pretty quickly with these results.
It's about time you did something useful with that car.
Nice job and great driving!
Looks like some idiot put way too much cage in that thing. Who would do such a thing??? lol. (I always joked that I figured I'd wind up on my roof at some point so I built the car accordingly). lol.
I'm really glad to see it win something, much less two races. That's an excellent update to the saga of the teal wonder.
That was great. You guys are very evenly matched. Great driving.
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